JBL 4408 Studio Monitors — Repairing the Woofer Foam Surrounds
In a former life, I worked in professional audio sales and service for a local music store. This was about a million years ago, and the store, Musicmakers Austin, is long gone. I was just recently out of college and the modest pay didn’t matter too much because I was living every musician’s dream: working as a musician — or at least in close proximity to working musicians. I worked mainly with keyboards and related equipment, selling dreams and repairing the equipment when the dreams failed. The modest pay was also offset by the opportunity to buy gear at a discount for my own studio — never mind that that further ate into my take home. In this fashion, I was able to equip my studio with keyboards, mixers, recording decks and sound systems. Heaven.
Many decades later, I still have some of that gear. It mostly still works even though much of the 80’s-era tech has been superseded by the modern miracles we use today. One thing doesn’t change though: the need for good studio monitor speakers. During the era I fell in love with JBL speakers and eventually paid too much for a pair of 4408 monitors. With an 8-inch woofer, titanium-dome tweeter and weighing in at 26 pounds, they’re substantial. Many mixes were made on these studio workhorses. Time had not been kind to them however, and parts deteriorated over the years. It’s a gradual thing, and one doesn’t realize it’s happening until something, like the foam woofer surrounds, develop cracks and then catastrophically fail. A sad day.
I had almost resigned myself to replacing them when an Internet search turned up a number of speaker repair options. Sending the 4408s to a Dallas repair shop seemed too extravagant. Then I discovered The Speaker Exchange. They provide reconing and other repair services for a range of classic speakers. I was especially happy to find replacement parts, including a woofer refoaming kit for my 4408’s now-destroyed surrounds. With parts available and videos showing the process, I was ready to start.
The $20 kit for the pair of speakers arrived in a few days. The process is straightforward and doesn’t require any exotic tools. Just a sharp utility knife and some patience. The old foam surrounds must first be removed. In my case they mostly just crumbled when I began cutting them away from the cone. Care must be taken to not damage the cone, or the repair becomes much more expensive.
Next, the outer gasket is removed by cutting the glue bead between the steel basket and the gasket. They came out easily, and much of the remaining glue can be removed with a scraper. I used an automotive gasket scraper with success.
Now, a bead of contact cement is applied to the outer edge of the cone, using the glue nozzle to spread the bead to the approximate width of the foam edge. The glue will become tacky in a few minutes, and you apply the new foam surround taking care to center it on the cone.
The dust cap is now removed. This is done by cutting a circle in the dust cap, just inside the inner edge of the cone. Extreme care must be used to avoid damaging either the cone or the tiny wires leading to the voicecoil. Once removed, the inner magnet piece and the inside of the voicecoil become visible. Four paper shims are now slid between the magnet and voicecoil. This is to center and stabilize the speaker assembly.
A bead of contact cement is now applied to the steel basket where the gasket was removed. Before pressing the outer edge of the new foam surround into the glue, it’s good to make sure the speaker cone is resting in a neutral position (not flexed in or out) by observing that the spider (the webbing between the outside of the cone and the inner part of the motor) is flat. The foam is now pressed into the glue.
After letting these glue joints dry for an hour or two, we can remove the shims and check to see that the speaker cone moves freely. Now, contact cement is applied to the edge of the new dust cap and pressed over the voicecoil to reseal the assembly. A piece of painter’s tape is helpful to hold and and apply the dust cap. Lastly, the gasket is glued back in place. That’s it!
It’s not a bad idea to apply a test signal to the speaker before reinstalling it into the cabinet. I used a function generator, but if you don’t have one, connecting the speaker to a sound system will suffice.
After years of marginal and sometimes ragged sound, the result was magic! In my studio, the 4408’s are driven by a Focusrite Scarlett 6i6 computer interface through a classic Dynaco 80 solid-state amp. I had forgotten how good the combination could sound. The speakers are arranged at a 60º spread and aimed at the mix position from their ceiling mounts — the perfect arrangement, and I spent the next several hours re-acqainting myself with their beautiful sound. Why did I wait so long to repair them?
Best $20 I’ve ever spent!
enjoy the music!
I already am!
Great write up. I’m curious though, how you mounted the speakers. I have a pair of 4312Bs I want to mount on the ceiling behind my garage bar, so that when enjoying a beverage the listeners are in near field.
Glad to hear you enjoyed it. The speakers are suspended from the ceiling on heavy duty “swag” ceiling hooks. If you look at the lead photo in the post, you may be able to see three stainless steel wires attached to screw eyes in the tops of the speakers. Those wires have a loop crimped in each end which joins the screw eyes to the ceiling hooks. If you choose this method, be sure to get the heavy duty hooks and not the decorative pressed metal hooks normally sold in home centers. The decorative versions will eventually fail with the weight of the speakers. I’ve had mine suspended on the heavy duty hooks for over 25 years now. Thanks for your comment and attention to the post!